So I got my new controller and the motor spins perfect when the self learning wires are connected. However when I disconnect the self learning and try to use the throttle in a very slow or any way the motor like jitters and stutters and create a vibration.
My controller can run without hall, so I dis connected my hall sensor and the throttle works except it moves backwards
Anyone have any ideas
My controller can run without hall, so I dis connected my hall sensor and the throttle works except it moves backwards
Anyone have any ideas