irvingoh999
1 µW
- Joined
- Dec 26, 2021
- Messages
- 1
Hi, I've recently upgraded my escooter's controller to a 18 Mosfet Bluetooth controller By Kunteng (KT) and also am using a KTLCD3. Everything is wired up properly, triple checked everything but the motor is spinning in the wrong direction and is drawing way too much current (20amps and above, tested using a clamp ampmeter).
I've also tried swapping the blue and green phase wires but the motor will not work after swapping those wires, makes a weird jamming noise. Any help will be appreciated, I've also tried changing some of the settings but the motor behaves the same way.
I've also tried swapping the blue and green phase wires but the motor will not work after swapping those wires, makes a weird jamming noise. Any help will be appreciated, I've also tried changing some of the settings but the motor behaves the same way.