Recently I bought a KLS7230S,24V-72V,300A for my E-Scooter with a 48V3000W hub motor.
Few days ago I hooked up everything and the hub motor is "running".
My problem now is that the controller goes into "internal error" when the hub-motor hits >400rpm.
Tried a lot of settings, but nothing seems to work.
Here's some more info;
Motor: 48V 3000W
Motor poles: 63
Motor magnets: 70
BMS: TinyBMS 150A
Battery: 16S23P, low=52V, High=64V (cells: panasonic NCR18650b)
Monitoring while running I see 5-10A phase current, motor hall sensors are showing up nicely, controller sees a nice battery voltage, motor identification is working, TPS pedal value is idle ~45 and around "internal error" point ~120.
One of the things which caught my attentions is the controller temperature is, seen in kelly windows application, bouncing between 0 and 251 (could this be a faulty temp sensor in the controller?).
Also i'm unsure on how to configure the "motor poles" and "resolver poles" values. For now these are configured at 63 (motor poles) and 3 (resolver poles).
Hope somebody is able and willing to help me
