Superwooper10
10 mW
So I know i'm new and all here, but I was scrambling around for hours trying to wonder why my wheel isn't listening to my bike anymore. I just took it to the bike shop to get it fixed because of a bent rim after getting out of a bad car wreck, and once it got back from the bike shop, the wheel refuses to move and just tries to take off, giving a violent thrust taking off one after another. When it gets up to speed, it sounds semi normal, but it's horribly making a noise as it tries to take off. When I let the throttle go, it sounds normal winding back down. Yet the 3rd error "Motor Hall Sensor Abnormality" is the reason it's giving the nogo. I did take the motor apart when I got that error and stayed up all night trying to fix it, but gave up. And just to recap, when I had it sitting at my house, I lifted up the front wheel and it spun up just fine on the bent rim. It even hit the top speed and gave no issue. But whatever this new rim is doing, this motor does not seem to like it and just won't play nice with it anymore. Please, is there anyone that can help wme with this issue? Do I HAVE to order new sensors with this new rim, or is there a way to recalibrate it or really try to fix it at home without spending more money on it? Do I need to replug with wires in a different way? (Yellow to green, blue to yellow, green to blue, etc..)The ebike display i'm using is a KT-LCD 3 screen and a 1000w motor.