casainho
10 GW
- Joined
- Feb 14, 2011
- Messages
- 6,058
So startup is rought and fast , low speed no possible. And asking all that current. I would say something about that angle is to much advanced.dr_lulz said:Motor runs but takes a lot of current. No load current is about 10A while it was 1A before. Startup is very rough and fast, low speed is not possible. I changed phase cables a few times but did not find a better combination. So this must be a software issue ...
any idea what i can do?
Please first do the procedure as described on install page, about verifying phases wirings and hall sensors wirings.
Then, please measure the output signal of the phase current sensor while motor is stopped. The sensor has 3 pins: GND, VCC 5V and phase current signal. Please measure it and say here what is the value.
Finally, I just can think of the adjustment of angle offset on config.h, that default value is 0. Try to increase/decrease in steps of 10.