buba said:I would of loved to hear some feedback of why this has happened and what the problem was exactly. I think there is something different causing the problem - not the previous code. Can someone else confirm the walk assist worked with high level of adjustability and precision and that it has suddenly changed in the last firmware changes? If this is the case even the Cruise function will not function properly so this leads me to believe this needs investigation.
I just got home from abroad and will try to test the firmware changes the next couple of days.
Hi, yes Buba, the previous version I had was your 0.18beta and walk and cruise were working ok.. not many test on walk assist as I had no chances to really push the bike up the hill, but the cruise was working the way I was expecting (I did not configured the target speed but just keeping the current speed).
Another thing I was seeing yesterday: I set assistance 1 to the minimum value 0.1 in order to reduce the gap while running with muscular bikers, and the motor power shown in the ODO menu 1.0 was 70-90 W..
I understood that the motor gives the human power*multiplier (0.1 in my case) but I really doubt I was putting 700-900W myself.
Did I understand correctly? Could you suggest some further checks to perform?
Or maybe the torque is not well calibrated?
Thanks